I know very little about the history of this generator, I bought it from GL a couple of years ago, dealt with a few typical minor issues to get it running. It is painted with solid green CARC and is missing most of the usual stencil markings, unit marking implies it belonged to a National Guard rapid deployment disaster response unit that was disbanded about a decade ago/ I don't have it in front of me at the moment, but think the indicated hours are around 2,000. This one has been sort of a back burner project, has always been hard to start, and smoked a lot off the end two cylinders until warm, I replaced in end 2 injectors with spare pop tested used ones I had on hand which helped a little. Yesterday I had it out of the shop in the sunlight, trying to load it down to test it, I found I had a little oil dripping out of the oil fill tube, upon adding load this got worse and smoke started coming out of the fill tube also. It will not take over about 7.5 KW load, at which point it starts loosing HZ, governor linkage (which needed repair) is at full and it still bogs down. After hitting this point 3 or 4 times over a 10-15 minute time period yesterday the generator shut off on overheat, but restarted after cooling down, it seemed warm, but not as hot as I would think it would need to be to shut down, so it could be a bad temp sensor, at this point I was loosing sunlight, so called it quits for the night.
Ike