mucekok
New member
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- Location
- spring, tx
finally got some motivation to get my most recently acquired duece to run correctly. originally had to replace injection pump and suspected a mistake in timing was causing the engine to run at full throttle. after coming dangerously close to scrapping the truck i found the throttle stop on the outside of the pump to be way out of whack. to my surprise the pump was timed right and it now runs correctly, sort of... here's the problem now... the blowby coming out of the crankcase vent tube is terrible! engine seems to have decent power but may have a slight miss just above idle. i am suspecting a need for valve adjustment, but that shouldn't have anything to do with crankcase pressure. i have no idea of the history of the truck, but am suspecting that it may have been an "ether-baby" and compression is suffering. i have not done a compression check yet so i am wondering if anyone has come across something simple that i am overlooking.