AtlantaSBR
Member
- 72
- 16
- 8
- Location
- Atlanta, GA
After driving my rig for a few months I recently started having some issues.
I replaced all the glow plugs due to the inability to start In cold weather and things we good for a while.
Replaced the fuel filter and separator after consulting the TM and then the issues began. It ran great for a few weeks afterwards and felt like it had more power than ever and then it began just shutting off at idle or while driving.
Currently no fuel will ever come out of the fuel separator drain when “idling” and I tested the output of the fuel filter and it doesn’t meet the spec of 1 pint while cranking for 30 seconds from the TM.
I have bled the system multiple times and if I unscrew an injector fuel does come out so hoping it isn’t the injection pump.
TL/DR; should I replace the fuel pump or drop the fuel tank and check for debris there? Worth changing fuel filter again after only 20-30miles? Any idea why my separator drain isn’t working?
Been scouring the TMs and the fuel pump seems to be the culprit but not sure if I am missing something on these old rigs. Also, the drain throws me off
I replaced all the glow plugs due to the inability to start In cold weather and things we good for a while.
Replaced the fuel filter and separator after consulting the TM and then the issues began. It ran great for a few weeks afterwards and felt like it had more power than ever and then it began just shutting off at idle or while driving.
Currently no fuel will ever come out of the fuel separator drain when “idling” and I tested the output of the fuel filter and it doesn’t meet the spec of 1 pint while cranking for 30 seconds from the TM.
I have bled the system multiple times and if I unscrew an injector fuel does come out so hoping it isn’t the injection pump.
TL/DR; should I replace the fuel pump or drop the fuel tank and check for debris there? Worth changing fuel filter again after only 20-30miles? Any idea why my separator drain isn’t working?
Been scouring the TMs and the fuel pump seems to be the culprit but not sure if I am missing something on these old rigs. Also, the drain throws me off