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Here is some info for anyone faced with this task. First of all, the purpose of the Cummins PT pump is to draw diesel from the fuel tank, and raise the pressure in proportion to throttle input, and send the higher pressure fuel to the injectors, where it is further pressurized for injection. If the pump is not working well, hard starting, low power and other issues can result.
In my case, the pump is equipped with an aneroid valve, which further adjusts fuel pressure based on turbocharger boost. If this valve is not working, the pump will never produce full pressure, and the engine will have low power.
I suspected my aneroid valve was bad, thanks to input from reb87 and others on this site. So I got busy and pulled the pump and sent it for rebuild. The task is simplified if you remove the fender, a simple 6 bolt task in my case (M915). To access the pump rear lower mounting bolt, I had to remove the power steering pump, a simple 2 bolt removal. The real trick to pulling the pump is the upper rear mounting bolt. This requires a 12 point, 7/16 swivel socket, such as a Proto 5274 (see pic). The rest of the task is very straightforward.
BTW, yes, the aneroid valve was bad, making my fire breathing Big Cam 400 perform like a wimpy 250. That problem is now behind me . . .
In my case, the pump is equipped with an aneroid valve, which further adjusts fuel pressure based on turbocharger boost. If this valve is not working, the pump will never produce full pressure, and the engine will have low power.
I suspected my aneroid valve was bad, thanks to input from reb87 and others on this site. So I got busy and pulled the pump and sent it for rebuild. The task is simplified if you remove the fender, a simple 6 bolt task in my case (M915). To access the pump rear lower mounting bolt, I had to remove the power steering pump, a simple 2 bolt removal. The real trick to pulling the pump is the upper rear mounting bolt. This requires a 12 point, 7/16 swivel socket, such as a Proto 5274 (see pic). The rest of the task is very straightforward.
BTW, yes, the aneroid valve was bad, making my fire breathing Big Cam 400 perform like a wimpy 250. That problem is now behind me . . .
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