USAMilRet
Member
- 390
- 15
- 18
- Location
- Tampa, Florida
OK, there seems to be a misunderstanding here. The generator and motor were not fully housed or put together when we came to the end result of the deal that I would get the refund. After that, it was just assembled as fast as it could be to get it on the road. Yes, they cheated on the gasket set and the use of the RTV and the missing gaskets. But otherwise than that, I was fully aware of the condition that the genset was in (of course I was expecting a clean gasket set and gaskets everywhere) and that it was not functioning the way it was supposed to be functioning.In my opinion you got reamed. Throwing an engine together with no gaskets, a clogged air filter, and gobs of RTV is a far cry from being a competent rebuild. If you are happy with it then great but I would feel cheated.
FYI, be mindful that those gobs of RTV can get into oil and water passages and ruin an otherwise okay engine.
I do not know what the original rebuild looked like, and it may have been just as bad, or I suspect that it was done rather well. The fuel cutoff solenoid failing, well that just happens. Return fuel line not replaced? Well, when does that ever happen. Leaky front seal...well that happens when you build tear down then build again. Sometimes seals do not get set right the second time. And that small bit of scaring on the seal......who would have ever seen that unless they knew what they were looking for. The undersized bolt in the head was inexcusable though.
Yes I am disappointed and frustrated the way the engine was put back together without a few of the upper gaskets and one lower gasket and with the use of "globs" of RTV cement. Truthfully, when we made the deal to do the partial refund, the engine may still have been partially apart at that time. He may also of considered it an AS IS sale like Gov Liq or IP or whatever, and considered this the end of it. I did not get that impression though.
I have seen worse...…..much worse...….then the overuse of RTV cement and missing gaskets. I do not think you guys are seeing the trees because of the forest and yes, I do know what RTV and STP and LUCAS and blah blah blah can do to engines.
You have to remember that all this started with IRMA last year and pricing has not subsided. The price I paid at the time is $3K to $4K less then what they were selling for after the VI and PR. So I have to tell you that I was pretty pleased to get the final down to $3500 for this genset.
He never wanted to sell this genset in the condition it was in and I asked him to sell it to me at the discounted price knowing it needed work because it was the one that I knew the most history about and had actually seen the inside of the engine through photos.
Yes Scott and I are going to have a discussion about these things, as we have had discussions about this genset before. I am pretty sure that if I ask for a gasket set because of this, I will get it for free. The rocker arm....that I can not explain and truthfully, we do not even know at this time if the rocker are breakage is a new thing or the cause of the problems.
I am not defending this particular reassembly of this particular genset. That put aside, the original low hour generator with 212 hours on it with the main bearing in it serviced, attached to a low hour original motor that has had all its wearable parts replaced, a new fuel pump, 4 new injectors, a complete valve job including grinding all surfaces and surfacing of the head with replacements of a couple of valves and all the springs, seals, etc..., new main fuel lines, new fuel filter, new oil filter, rings, bearings, seals, piston pins and bushings, new water pump with new hoses, on an engine now with 15 hours on it that a lot of people are pretty sure that the rocker arm replacement will fix all the problems.
To me, this is a extremely low (212) hour generator married to a newly rebuilt (15 hour) engine in a shell where every missing screw and nut was replaced with the proper sized original. Now I know that Scott had a mechanic that he was using to do the engine rebuilds so for me, it is hard to blame the owner for the action of the employee (if the owner is unaware) of the actions. I also know that the head was sent out to a machine shop for servicing. But I will have discussions about his mechanic and how this all looks very bad for his business.
YMMV