So, today I got everything connected and put back together on the Gen Set. I put in new Wix filters (spin-on), primed all the pumps and fuel line up to the 90 just upstream of the check valve. I drew 2 1/2 gallons of fresh fuel into the day tank using the Aux Pump without issue. I then turned the Master Switch to Prime and let it run to check the flow in the Return Hose and to push out any old fuel past the check valve's upstream 90; the Return Line had small but solid stream of fuel that I had flowing into a waste bucket...I also took this time to look for any leaks and I didn't see any. I turned the Master to off and connected the Return Line to the day tank.
The anticipation was killing so I tried to start it....It' alive!!!! It fired right up, no knocking, no fluctuating RPM's and no smoke. I watched and listened to it for about 15 minutes, and it was running great BUT THEN,,,,,RPM's slowed, it started to knock and produce gray/white smoke, so I shut it down. Within about 10-15 seconds I was going to try to start it again, so I turn the Master Switch to Prime and clicking was rapid then slowed as if it hadn't been running; it's been my experience with this unit that if I shut it down and restart it relatively quickly the pump clicking is pretty slow, I assumed it was because it still has pressure built up in the system but that's just my guess. With the Master Switch still set to Prime I look at all the fuel connections and found one leak; it was at the 90 that the inlet side of the Check Valve threads into...it wasn't spraying but it was more than just a drop, drop.
Think the leak could cause it die off like it did?
I ran out of time today, so I'll fix the leak tomorrow.