Had a few hours to burn tonight, so I pulled the HH. The button and 3prong clip were still attached like they should. The plunger guide’s writing was facing out like mentioned above so that was good. I disassembled everything again and cleaned it. All passages were free and clear and flushed nicely. I reassembled everything. Took it to the truck, lined up the red tooth and the pointer, and it dropped right in. Bolted everything down, and reinstalled all the lines.
Turned on power, cracked the fuel line at the HH inlet. Bled until I had fuel. I left power on for 5mins to cycle fuel. I then cracked the 3/4” bolt on top of the HH, with power on still, I got a few dozen small air bubbles. Once it cleared i tighter it down. I then let it sit and cycle for another 3-5mins.
I cranked and cranked, but I was being easy on the starter also. 10secs here, 15secs there, then take a break. I always kept the power on during this whole time. I tried maybe 20 times; crank no start.
This time I had NO vapor/smoke from the stack.
I took about a 10min break because I was getting frustrated. Came back, decided to crack and remove the #3 injector line at the HH because it’s the easiest to get to. It was completely removed, I cranked and cranked. Absolutely NOTHING came out of that injector hole, but I know for sure it flows good and isn’t clogged.
It’s very late and I gotta work in the AM. I’m defeated for the evening but I guess there’s always tomorrow.