Ok...
Ran the purge through it today. Ran half of it at no load... half at 4kw load. No real change but the fuel that was returning definitely changed color.
After letting it sit for a bit after the purge, I ran it for an hour with a 33.8a load. Runs smooth and clean. Tried to throw the last breaker and its the same.
Then adjusted droop ad the manual says. It took quite a bitnof adjustment to get to the point where it would hunt/surge under a light load. Backed it off until it stopped hunting. Fired it up and now its worse.
Frequency doesn't drop as much but now it won't hold an 8100w load as it did before. Stalls out like it was doing with all 3 breakers flipped.
I started looking at the linkages and its almost like the IP has a bit more throttle to give but the plunger on the linkage bottoms out. This is while moving by hand. Not sure how it operates while being worked by the governor.
Checked fuel supply through the filters at the IP supply and it'll fill a 20oz bottle in a few seconds. Plenty.
Whats also odd is that when applying loads, there's no haze at all .. I would expect it to puff a little as the load is applied .. but rpm just drops and then recovers as if it isn't getting enough fuel to prevent the rpm drop.
Digging back into the TM
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